Ultra-high performance, yet rather simple - hybrid and more!

TubSumo

Hello Valery,

I've received the TubSumo PCBs from Terry (thank you Terry!) and am gathering parts to build. I've got a tube of ALF16N16W/ALF16P16W lateral power FETs that I would like to use. Would you expect a problem to use them?

I've got both +/-55 volt and +/- 72 volt ConnexElectronic switching power supplies on hand. Which would be the preferred voltage? I anticipate bog standard 8 ohm loads. I vote for 72 volts. What are your thoughts?

Any mods to these PCBs that I have missed? I am not aware of any.
 
Hi Carl,

Good 🙂 I didn't try Exinos Lat-Fets, although I don't see any issues with them. I will check the situation with input capacitance for them - K1058/J162 have got noticeable difference, so we have to use additional caps to balance it out.

If you go for the tube input, +/-72V DC rails are the right ones.

No PCB mods required, just if additional caps will be used at tha gates, the right position will be gate-drain - don't use gate-source places on PCB, place them directly on fet pins.

I will check the situation with Exinos fets' capacitance later today.

Cheers,
Valery
 
Wow! 😱

ALF16N16W/ALF16P16W ones have got input capacitance at least twice as much comparing to Hitachi/Renesas ones.
900pF / 1850pF respectively, according to the datasheet.

That means, you will have to put 910-1000pF capacitors G-D for N-channel fets.
It will probably make sense to decrease the gate stoppers' value down to 220R, sovthat the time constant stays roughly the same.

Anyway - it will be a useful experience 😉

Cheers,
Valery
 
I must say, now that I know that the oscillation was caused by the capacitance offset in the OPS my IPS is back to the stock values. I have ordered some more boards because I want to try the FET version. I will have some extras for those interested. These are the latest version with easier to read screen print.

Valery,

I noticed that this amp doesn't seem to have the huge rail swing that the Low TIM has. It only has about a 2.5V offset at initial startup where the Low TIM has something like 32V offset.

Another thing I found is that after I got everything working I was able to get it to run fine with the JJ tubes.

Blessings, Terry
 
I must say, now that I know that the oscillation was caused by the capacitance offset in the OPS my IPS is back to the stock values. I have ordered some more boards because I want to try the FET version. I will have some extras for those interested. These are the latest version with easier to read screen print.

Valery,

I noticed that this amp doesn't seem to have the huge rail swing that the Low TIM has. It only has about a 2.5V offset at initial startup where the Low TIM has something like 32V offset.

Another thing I found is that after I got everything working I was able to get it to run fine with the JJ tubes.

Blessings, Terry

Hi Terry,

Thank you for the info - always good to know.

You are right, the startup swing is much lower - it was one of my initial requirements for this design - highly symmetric topology allows low offset even before NFB is fully operational.

I also like very clean measurement curves here, as you mentioned earlier, as well as excellent temperature stability 😉

Cheers,
Valery
 
OPS . Need cleanup
 

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Hi Valery,

The Low TIM hybrid is a very nice amp as well. If you ever get around to doing a new layout for that one, maybe you could fit it on a smaller board like this and with the terminal order to match.

Blessings, Terry

Agree, I especially like that one with Hex-Fet OPS.
I have actually started re-arranging its PCB - will try to finalize over the weekend 😉

Cheers,
Valery