Power amp measurement system

G10 post-notch preamp. IMHO it has quite good performance.
 

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I made a compact version of the post-notch preamp. Same box (enclosure) as for notch, powered by external batteries. Gain is selectable by jumper, 1x or 100x. The PCB has two versions, one for single op-amp (OPA627,827,828, etc) and another for dual op-amp (OPA1656,etc). On the picture you can see boxed OPA827 with bypassed input/output caps (4mV output dc @40dB) and unboxed OPA2141 version (waiting for OPA1656). Second picture captures OPA827 output noise (amplification 100x) , input impedance is 50R.
 

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Almost finished voltage divider, AAA battery holders are on the way, till arrive I made a battery pack (white color on the picture).
The front board holds the divider/attenuator, mosfet SSR, mosfet driver while the rear one is a protection logic/driver.
 

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The test ( 1uF was replaced by two 2u2 in series)

I use manual fundamental in REW. The graphs do not take into account the behavior of the passive filter on H2,H3 ...

1/ LPF is not used

D10s -3dBFS (1.42Vrms) -> Passive notch filter -> Post notch AMP +40dB -> Cosmos ADC unbalanced 1.7V range


D10s-3dBFS - Pnotch1k - AMP+40dB - Cosmos no-Hx-comp.png



After the passive filter correction we get

H2 = -158 + 9 = -149 dBc
H3 = -139 + 6 = -133 dBc


2/ LPF is used, powered by two 9V batteries

D10s -3dBFS (1.42Vrms) -> LPF -> Passive notch filter -> Post notch AMP +40dB -> Cosmos ADC unbalanced 1.7V range

D10s-3dBFS - LPF - Pnotch1k - AMP+40dB - Cosmos no-Hx-comp 2u2.png


After the passive filter correction we get

H2 = -162 + 9 = -153 dBc
H3 = -153 + 6 = -147 dBc

Nice !
probably a better quality C1 would give a lower H3
 
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