Could anyone please help me ID source of -3db @20Khz in Schematic?

Ciao, op-amps - dont need you and your interference.
This is unfair and unwarranted.

It is NOT an OpAmp problem, at all, but poor implementation and/or: User Error.

Improperly using that balanced input makes the useful 330pF RF interference capacitor into a 20kHz |attenuator.

And even so ... guess 10 to 20db less than typical user attenuation at that frequency.
 
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I explained it in posts 54 and 57, but I guess I'm on the ignore list.
No, I simply didnt get to read it before posting the FR performance of the test interface, as that seemed to be requested many times here. Then, instead of leaving the post at that, I blathered on about the circuit. Sorry...I do appreciate all of everyone's effort to right my understanding fo what's happening here!

I initially had the opposite input shorted, then later removed it thinking it wasnt needed, as there's a bleed resistor to reference to ground there anyway. Let's see if the op-amp diff to SE converter measures properly with the (-) input dead short to gnd, signal going into the (+) side.

My mistake, not understanding how to wire a SE output properly to a balanced input. Actually I did understand at first, but then overthought it in grasping at straws.

The NRV10 has balanced outputs and I could have wired up a couple canon connectors for the initial listen; but, I thought, I'll never use the amp that way, only with SE outputs, so why bother.
 
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I see. It is the combination of the open negative input and the way the 330 pF has been connected that causes most of the roll-off, the open negative input would not have caused any roll-off if they had used two equal capacitors to ground instead.
 
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I hope this shows that it's not the measurement system.
This loopback measurement does not show this heavy roll off at 20kHz from first post.
IMHO the rane amps do not have such a ultra high deep supa dupa filter at 20kHz.
Was the sampling frequency in both measurements above 96 khz and no digital filter active? deemphasis deactivated et al?
BTW, measure 3times: loopback, left and right from the output inductor with same settings.

Have fun, Toni
 
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This loopback measurement
Please read #51. (I don't know how we got to 50 posts without this key clue.) It never was "loopback error", and we knew that was unlikely from #1 ("another SS amp" showed no rolloff). But there was a whole other stage in front which did an unexpected thing when connected unexpectedly.

Old wire-benders like me might have thought to hard-reference the unused screw. A transformer input would have gone very wonky. But who uses transformers? Or understands how the RF cap cross-talks the diff-amp above 10kHz?
 
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This time I made sure that ground jumper has continuity by explicitly checking across the pins with my meter. I may very well have gripped the wire jacket with the screw-down jaw of the connector in my previous SE to Bal connection attempt.

Going across all 6 amplifiers, each measures 20-20k -1db at each end of the spectrum. I for one did not "understand how the RF cap cross-talks the diff-amp above 10kHz" until going through this exercise. Now I know and hopefully remember this experience.

I had a listen tonight - same. Confounding things, I suspect the tweeters on the HLS 610s are blown. Imagine a timeline like;

Joe burns his tweeters, but doesnt know it --> gets new amp, doesnt sound right --> measures an erroneous connection's effect he doesnt understand how could possibly be --> ascribes sound to measurement --> posts in DIYAudio about it --> ratifies his measurement equipment --> gets straightened out why this particular balanced input circuit with lopsided connection...-->fixes input connection, all re-measures as OK -->still doesnt sound right -->other Kenwood amp doesnt sound right now, either.

The HLS are hanging from the rafters. If I go up there on a ladder to pull out the connector panel / crossover and measure the tweeters continuity, I just might fall off and really have something to write about. I do have replacement tweeters and I dread taking those back down, but I've had enough circuit sleuthing for one weekend.

Playing around with 100 WPC amplifiers with no input level controls...well, lets just say that screech I heard when the Kenwood was connected as the RCA cable pulled itself out of the RCA to 1/4" adapter in the back of the NRV10 - probably could have done it. I swear I connected the Kenwood back up in the middle of that timeline and it was sounding fine through the HLS; but maybe I only measured it.
 
I think I'll put some pink noise through these speakers and hold up a measurement mic into a 48th octave analysis - while standing on the floor - much safer approach. I really have to watch the attitude with which I get up on a ladder; exasperation around what's happening isnt a good mode to be up on one of those...
 
If you measured with a resistive load and if it gets flatter with higher load resistance, then it must be L3.
While checking each amplifier with the unused side of the balanced input properly grounded, I did put the two 8 Ohm loads in series and measured the last one again. It was about the same; even though I now know that L3 is not the issue, I did the experiment anyway.
 
I think that the lifelessness comes from overprocessed gain structure and complex compensation to provide stability. Also, that bootstrap execution looks like positive feedback to me, which in turn demands even higher stability measures.... just to prevent oscillations. But, only one half of the sinewave is bootstrapped..?? No? It would be interesting to load the amplifier with various types of load (R/L/C) and look/check for the symmetrical or non-symmetrical clipping/behaviour... These loads should be connected with the intended speaker cables in place... to count for the cables' capacitance/inductance.
Interesting. The amp has switches so someone can run two amps in BTL for 300W supposedly; perhaps the bootstrap isnt "only one half of the sinewave" in that mode? A mode I'll never use and an output voltage level I'll never take it to where the driver transistor needs a supply greater than B+.
 
I made a simulation of the circuit using parts that
I had models for and only saw a .5 db drop at the output
before the inductor. I had to make the output inductor
50 uH before I could get a 3 db drop at 20 KHZ.
Output inductors are not usually that big!
Thanks for doing that. You can see in the board photo the inductor. Now I cant tell inductance from physical size / turns in air, but I think this is element getting ruled out!
 
Something with such a strong lowpass filter may very well start dropping above 10kHz, and in that case, the dropping curve can very well be caused my the Soundcard (measuring instrument) itself and not be present on the amp per se.
I have a Focusrite Scarlet solo, which I havent setup yet for doing audio signal measurements. When I do, the brick wall filter around 20k wont be a concern. My next focus will be getting the harmonic distortion spectrum response and the Focusrite with its much better sampling performance will allow me to see some of those out to 20k. But tomorrow I'll use it to verify my blown tweeters, vs ears / brain.
 
Even after pulling the opamp you're still down 1.5-2 dB at 20 kHz. I would have expected more bandwidth from the amp.

I would also have expected more bandwidth from the balanced input (which is worth retaining). It's a 14 MHz (typ.) opamp (10 MHz w/c).

If you decide to make this modification permanent, you might want to solder a wire onto the bottom of the board instead of relying on wires stuck into IC sockets.
The designers didnt seem to have any qualms about how many op-amps or caps the audio signal went through. I'm still on the fence, but I'll probably just leave the balanced input intact - even with its idiosyncrasy when driving single ended signals.
 
A good lesson to always use volume control as it is a kind of fuse.
The particular Kenwood amp doesnt have one - just the RCA input and speaker outputs. Was planning on drilling a hole in its front panel (I got it for $5 at the goodwill outlet, cover is is a little too bent up to sell; judging by the price they go for, no one would want it anyway so who cares?) and slamming something in there, but never got round to it - and now this.

By acoustic measurement and comparison with a known good speaker, the HLS tweeters are dead. Dammit. The coincidence got me all suspicious about this Rane amp, when it was something else altogether. I guess we can add deaf, to dumb and blind.

Gone.jpg


I noticed in one set of xovers I've dismantled, they used incandescent lamps (in series) as tweeter protection. Better to light up one of those, than the tweeter VC on accident. I'd like to add something to protect my last tweeter set when I repair these. The Rane has volume controls per channel so it's a bit safer than that Kenwood.