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#321 |
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diyAudio Member
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Not questioning H2 cancellation, which is not that easy to achieve in practice. I was just using empirical data to demonstrate that actually 4P1L is more linear than 6C4C.
Ale
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"A mistake is always forgivable, rarely excusable and always unacceptable. " (Robert Fripp) http://www.bartola.co.uk/valves/ |
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#322 |
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diyAudio Member
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Quote:
I wouldn't run the 4P1L at 325mA filaments as H3 increases significantly and linearity goes down the toilet when swinging large signals. 350/360mA in my experience is the minimum... Ale
__________________
"A mistake is always forgivable, rarely excusable and always unacceptable. " (Robert Fripp) http://www.bartola.co.uk/valves/ |
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#323 | |
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diyAudio Member
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Quote:
Ill post bigger screenshots in time, right now still looking at the GU-50 vs 6C4C vs PSE 4P1L for the output. Back to the 4P1L, thanks for the tip about the filament. I agree that it is inherently more linear than a 6C4C up to a point. For my case where I am driving 2 watts into 38 ohms I need to swing a lot of volts across the primary, almost as many volts as an 8W 300B output. So the 4P1L just may not have a high enough plate voltage to work as an output tube for my 2 watts, but it is looking perfect as a driver. Unfortunately my transformer models are the limiting factor here ( I can't figure out how to model the -0.8dB insertion loss of the LL1623. I could upload a zip of all my sim files including the LTC program on a file share site and you could start simulating with a few mouse clicks. shoot me a PM if you like. The output transformers are really the frustrating part of designing an unusual SET headamp, almost need to buy the OPT's first, test them for inductace, loss, DCR, etc then choose your tubes & power supply operating points ! |
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#324 |
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diyAudio Member
Join Date: Sep 2003
Location: London
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Are you running the 4P1L in series or parallel filaments? Looks like series. I'd run them in parallel at 1.9v. Smaller cathode resistor in filament bias.
Don't neglect to try 4P1L in filament bias on the output. I started with 6C4C with bypassed cathode resistor as you show, and much preferred 4P1L in filament bias. Getting rid of the cathode bypass lifted a veil. In particular the piano sound is incredible, and if you like piano you should hear it. |
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#325 |
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diyAudio Member
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http://www.diyaudio.com/forums/attac...l-ll1660_3.png
Wich values for grid resistor and input to gnd resistor? |
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#326 |
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diyAudio Member
Join Date: Sep 2003
Location: London
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Whatever you like in the usual range - maybe 1K grid stopper and 470K to ground. Opinions vary on these things, so I wasn't precise.
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#327 |
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diyAudio Member
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Thanks Andy.
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#328 | |
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работник
diyAudio Member
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Quote:
Yes, if the 47K grid resistor is moved to connect across the CCS only - then connect one end of the IT secondary to the bias, the other end to the grid. No other connexions at the grid needed. This way, the grid sees the bias voltage, but the IT winding feels none of the dc current. With a high quality IT, this will give an excellent solution! |
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#329 |
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diyAudio Member
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I just noticed that the LTspice model I use for the 4P1L is modeling 2 in parallel, does anyone have a model for a single?
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#330 |
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diyAudio Member
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Is actually Dmitry's composite model which is more accurate:
Composite Tube Models
__________________
"A mistake is always forgivable, rarely excusable and always unacceptable. " (Robert Fripp) http://www.bartola.co.uk/valves/ |
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