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#1301 |
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diyAudio Member
Join Date: Dec 2009
Location: Great Falls, VA
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AndrewT,
Here is clipping at 3% THDN. Neel |
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#1302 |
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No snake oil
diyAudio Member
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ndepot,
Yes, about the same 1KHz performance as the wire (opc:s measurement). Not bad for a 30 year old design. Sub 0.1% at 300W 100kHz is impressive (I think). I will soon build a soundcard interface. With current soundcard in loopback 3:rd harmonic dominates at -100dB so it will hardly be sufficient (measuring 3:rd) for this kind of amp. However rest of the harmonics is down at -110db, noise at -120dB so maybe I'll see someting. ![]() I hope we will se a lot of measurements, it’s quite revealing.
__________________
/ Anders |
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#1303 |
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diyAudio Member
Join Date: Dec 2009
Location: Great Falls, VA
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The LME supply is +/- 65V from HP regulated power supplies. Owen's board has additional capacitors for isolation and noise filtering.
The transformer >1KVA Smoothing caps are 72,000 uF for each rail, plus 1000 uF more per rail on the board. I believe that we can rule out the transformer. |
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#1304 |
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diyAudio Member
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Hi,
frequency of the input signal? Last edited by AP2; 18th May 2012 at 09:07 PM. |
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#1305 |
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diyAudio Member
Join Date: Jul 2004
Location: Scottish Borders
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Can anyone account for the flat tops of the clipping not being at the top?
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#1306 |
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diyAudio Member
Join Date: Dec 2009
Location: Great Falls, VA
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AKN,
I would like to know more about your soundcard analyzer project. |
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#1307 |
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diyAudio Member
Join Date: Oct 2004
Location: Ottawa, Ontario, Canada
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I have no idea why the clipping looks like that... I've never seen that before, and my measurements here don't reflect that.
I'll test in a few minutes and report back. It almost looks like the power supply begins to collapse at the peak and doesn't recover until the load is lightened. I think AndrewT might be on to something asking about the supply and the transformer, but npdot's setup seems pretty hefty. I'll post measurements in a little bit with the DPS-600 Cheers, Owen |
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#1308 |
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diyAudio Member
Join Date: Dec 2009
Location: Great Falls, VA
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Andrew,
Just brainstorming: 1. Output device transconductance droop due to current surge 2. Output device transconductance droop due to rapid changes in die temperature. 3. ?? |
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#1309 |
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diyAudio Member
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please, change f of input signal 10x high and show clip.
if you change f eg. low (150hz) and (clip angle) moves to counter-clockwise, then is a problem on psu Last edited by AP2; 18th May 2012 at 09:21 PM. |
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#1310 |
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diyAudio Member
Join Date: Dec 2009
Location: Great Falls, VA
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AP2,
Signal is 1KHz. |
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