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#1 |
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diyAudio Member
Join Date: Jul 2003
Location: Dayton, OH USA
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Thorsten,
I have simulated several phono EQ circuits you've suggested at various threads here and they all have about 1.5 dB error from 20hz to 20kHz. Signal at 20kHz is off by almost 2 dB against 20Hz. I used HagTech schematic to implement reverse EQ circuit: Hagerman Technology LLC: iRIAA Filter for Phonostage DIY Kit I run several other phono circuits through the same simulator and they have much lower error. Here is the simulated schematic: http://dl.dropbox.com/u/17742412/Phono%20sch%202.jpg EQ error: http://dl.dropbox.com/u/17742412/EQ%20Curve.jpg Pay no attention to absolute gain values on EQ error chart as V/I stage gain is very low. Any ideas of why I get this much error? Are you using a different EQ from standard iRIAA? Thanks Sergy |
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#2 |
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diyAudio Member
Join Date: Jul 2003
Location: Dayton, OH USA
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Re posing massage with visible images attached:
---------------------------------------------- Thorsten, I have simulated several phono EQ circuits you've suggested at various threads here and they all have about 1.5 dB error from 20hz to 20kHz. Signal at 20kHz is off by almost 2 dB against 20Hz. I used HagTech schematic to implement reverse EQ circuit: Hagerman Technology LLC: iRIAA Filter for Phonostage DIY Kit I run several other phono circuits through the same simulator and they have much lower error. Here is the simulated schematic: ![]() EQ error: ![]() Pay no attention to absolute gain values on EQ error chart as V/I stage gain is very low. Any ideas of why I get error this big? Are you using a different EQ from standard iRIAA? Thanks Sergy |
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#3 | |
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Previously: Kuei Yang Wang
Join Date: Nov 2002
Location: Somewhere nice on planet earth
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Hi,
Quote:
Ciao T |
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#4 | |
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Previously: Kuei Yang Wang
Join Date: Nov 2002
Location: Somewhere nice on planet earth
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Hi,
Quote:
Also try converting the circuit to "generic" that is make the first amp a normal non-inverting one and then use a pair of 1K5 resistors with the 100nF cap to ground from the junction, instead of the 750 Ohm and Howland current pump. This will remove the various interactions you are seeing... Ciao T |
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#5 |
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diyAudio Member
Join Date: Jul 2003
Location: Dayton, OH USA
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#6 |
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diyAudio Member
Join Date: Jul 2003
Location: Dayton, OH USA
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#7 | ||
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Previously: Kuei Yang Wang
Join Date: Nov 2002
Location: Somewhere nice on planet earth
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Hi,
Quote:
This particular Phono design I originally simmed in Tina TI which includes all the Op-Amp models etc. Quote:
The remaining rolloff is still too much, with the 33R resistor in series with the 100nF Cap I'd expect to see some HF Boost. Could it be that the fairly slow Op-Amp's in your simulation contribute to the early HF rolloff? Ciao T |
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#8 |
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Previously: Kuei Yang Wang
Join Date: Nov 2002
Location: Somewhere nice on planet earth
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Hi,
I had a look for the original work I did on this, but it seems that this was one of the few areas of my laptop that was not backed up anywhere when it was stolen a few weeks ago. So I re-created the circuit I used as best as I could from memory, it should be mostly accurate (see attached). There is a small correction to the 750R resistor in the EQ, as the implementation of the HCP I used has a finite (but well defined) output impedance, so we need to increase the 750R to compensate. As shown gain is 66dB. Noise around -76dB re. 0.5mV. The HF rolloff in the simulator is, I think, an artefacts of the Hagermann network vs. others. The actual unit build measured better than +/-0.1dB from flat response and equal levels of channel imbalance without any selection using the AP2 at work. It seems AP disagrees with JH on what the RIAA curve is... The actual unit build used NOS East German Mil-Spec 0.5% Polystyrene & Tinfoil Cap's (plastic encased) and 0.1% metal film resistors. Also not shown, the offset trim is manual via the Offset pins on Op-Amp's, but I would probably expend an OPA627 on a servo instead if I where to make another one like this. Not shown are the power supplies, overkill dual mono, with 4pcs 120VA Torroid transformers, 10 * 10,000uF per rail in CRC filters followed by a Darlington Capacitor multiplier followed by 80uF/35V Film Cap's plus the rest of the usual decoupling... Ciao T |
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#9 |
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diyAudio Member
Join Date: Oct 2007
Location: Vienna / Austria
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Hagermann advocates the non standard "Neuman Pole" I believe, this might explain the error at high frequencies. (Which isnīt an error actually).
__________________
Regards, Georg |
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#10 | |
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Previously: Kuei Yang Wang
Join Date: Nov 2002
Location: Somewhere nice on planet earth
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Hi,
Quote:
So, one mystery less. Ciao T PS, I neither per se advocate or detract from the "Neumann" EQ, I do prefer to listen with it included though, as do many others we tried this with (including blind) |
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